What a day yesterday out at DSG. The plan was for me to install a TXS TMIC before heading out there and they were to cut out the 3" - 2.5" taper at the end of my cobb dp, weld in a flange, bolt up a 3" cbe and tune the goods. Got the new interwarmer last week, opened up the box and it just didnt look right, brackets were off, silicone hoses werent correct and my cast y-pipe didnt match the flanges on the under side of the txs. So I called up circuitmotorsports and got an rma number on. Getting ready to leave yesterday morning and I say, what the hell, I'll bring it with me and see what they say.
Got there at 10, they bring it in, cool down time, chit chat, jack it up etc...
Old Hayward and Scott comes off

, love that sound, dp off, over to the bench, chop chop, back on. Done.
Dyno time!
Matt gets set up, warm up run, all is well. We head into the office cause it gets loud as hell when tuning inside.
1St pull, he gets to about 5K and, boost leak!
IC comes off, tightened down the four y-pipe bolts, snap. Cast piece busted on both sides. Back over to the bench. Turns out it does need wrx cast pipage cause the flange thickness is different, luckily they have a set lying around. So now he has to use the shitty silicone y-pipe that came with the txs and it barely fits over the blouch outlet.
Matt does a warm up, 2nd pull, coming into boost, SCREACH. Nick's like WTF. Had to double up with gaskets on the bypass. 3rd pull, money, all sealed up.
So were in the office having lunch while Matt is doing pulls 4-11, all is well.
Pull 12, matt shuts down a little early.
He says 2 pulls earlier, boost came on 800 rpm late, and that the last pull was 800 rpm later than that. He lets it cool down for about an hour and tries it again. No boost till 6K, shuts her down, Done.
At this point its like 4. For the next hour they ruled out all other possibilities without actually taking the turbo off for inspection. Turns out that oil is leaking into the compressor housing, ? bearing failure. So I limp my ass the 3 hours home on wastegate pressure only, stopping every half to 3/4 of an hour to check the oil and constantly pearing back for black smoke.
Turbo was installed on 5/20 and has seen 2700 miles of moderate use.
On a good note, made 316 wheel with a failing turbo